My car weighs 3300lb w/driver, has a stock 4-speed, uses a pump gas 302 with 289 heads that I ported myself without the aid of a flowbench, stock cast iron crank, 289 rods and TRW pistons. The engine has a solid flat tappet cam (Comp 282S magnum lobe on the intake, 294 exhaust) measuring 236/248 @ 0.050", and is shifted at 6800 rpm. It has seen WAY more street than track time, and has proven to be very reliable over the years.
It still has the heater, wipers, stereo, lighted make-up mirror, carpet, etc. It was driven 100 miles each way to a cruise-in shortly before removing the engine.
Come race day, the pump gas gets replaced with whatever race fuel is available, and the bottle gets turned on.
The car is set up for nitrous, and ran the times below with it. I rarely get to the track, so most of the runs have been on the bottle. On the 1/8 mile, it did manage a 7.48 without the juice. It ran 6.74 @ 103 with the bottle on the 1/8 mile.
When the engine was 'fresh' it ran 6.74 @ 102 on a 150hp shot. As it wore, the nitrous was turned up to 200hp, and it ran the same et at 103. The day before I took the engine out, the pistons were slapping in their bores, but it still managed a 10.65 in the 1/4.
It's not an optimized race car, but does okay for what it is. It's just an old school truely streetable hotrod.
For the curious, on the way to the track (the last time where it ran the 10.65) the car got rear-ended. I still ran it, even though the rear frame was bent and it spewed gasoline out the back on every launch. I came home and did some 'end of the season' nitrous testing without the proper fuel. It was a bad idea, since a couple pistons decided to break off at their ring lands. I took it as a good opportunity build another engine, which will be up and ready this spring. The short block is ready, and awaiting me to finish porting the twisted wedge heads. It will also be a pump gas, street 302. The car has been on a frame machine, and is awaiting bodywork.
It was a pretty sucky weekend... going from a fully functional 10 second, fairly good looking mustang, to a crashed up car with a blown engine.... all in the course of two days!
After pulling the heads, I mailed one to a guy who wanted to use it as a model to port his. In exchange, he took it to have it flowed. With an old beat up valve job, the intake flowed 218, the exhaust 176.
Oh well, it won't be long til' it hits the road again.
Good Luck!